Hi, I’ve purchased the board and it’s been nearly 20 days the whole board was working fine reliably accurate IMU data, but all of a sudden the yaw data reacts to the change in IMU but goes back to the same place eventually
. The board was not damaged either physically or no chance of static discharge too. The Roll and Pitch data seems accurate but the yaw data keeps messing up. I only need the yaw data the most, need help with this.
I’ve tried,
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Reuploading the firmware.
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Ensure no emf is causing this issue.
Need help, Thanks in advance.