IMU glitch on the Sparkfun Openlog Artemis DEV-16382

Hi, I’ve purchased the board and it’s been nearly 20 days the whole board was working fine reliably accurate IMU data, but all of a sudden the yaw data reacts to the change in IMU but goes back to the same place eventually
IMU_glitch.gif. The board was not damaged either physically or no chance of static discharge too. The Roll and Pitch data seems accurate but the yaw data keeps messing up. I only need the yaw data the most, need help with this.

I’ve tried,

  1. Reuploading the firmware.

  2. Ensure no emf is causing this issue.

Need help, Thanks in advance.

Hello RoopanJK,

You have now asked the same question in three different places. I replied to your first question. Please do not ask again.

Best wishes,

Paul

I just posted in 2 place, here and a github issue!..Please direct me to the answer!.

Thanks.

You asked twice on GitHub. Here is the answer:

https://github.com/sparkfun/OpenLog_Art … 1398010827